湖南电力 ›› 2022, Vol. 42 ›› Issue (2): 80-84.doi: 10.3969/j.issn.1008-0198.2022.02.015

• 经验与探讨 • 上一篇    下一篇

油浸倒立式电流互感器缺陷分析及对策

徐鹏, 崔光鲁, 甘强, 陈昊, 张海华, 谭风雷   

  1. 国网江苏省电力有限公司超高压分公司,江苏 南京 211102
  • 收稿日期:2021-12-08 修回日期:2021-12-24 发布日期:2025-08-05
  • 作者简介:徐鹏(1990),男,工程师,从事高电压与绝缘、电气设备故障诊断。
  • 基金资助:
    国家自然科学基金资助项目(51807028)

Analysis and Countermeasures of Oil Immersed Inverted Current Defect

XU Peng, CUI Guanglu, GAN Qiang, CHEN Hao, ZHANG Haihua, TAN Fenglei   

  1. State Grid Jiangsu Electric Power Company Limited Super High Voltage Branch Company, Nanjing 211102, China
  • Received:2021-12-08 Revised:2021-12-24 Published:2025-08-05

摘要: 针对500 kV油浸式电流互感器批次缺陷展开调查,通过诊断试验和解体分析综合研判该电流互感器缺陷的主要原因为器身与储油柜之间的挤压、摩擦造成局部皱纹纸损伤,在高频过电压下,局部皱纹纸发生击穿产生乙炔。最后提出相应的建议措施,为同类型电流互感器的故障诊断和运行维护提供参考。

关键词: 油浸式电流互感器, 故障成因, 批次缺陷, 故障诊断

Abstract: In this paper, the batch defects of a 500 kV oil immersed current transformer were investigated. Through the diagnosis test and disassembly analysis, the main reasons for the defects of this type of current transformer are found to be the local wrinkled paper damage caused by the extrusion and friction between the body and the oil conservator. Under the high frequency overvoltage, the local wrinkled paper breaks down to produce acetylene. Finally, the corresponding suggestions and measures are put forward to provide reference for fault diagnosis and operation maintenance of the same type of current transformer.

Key words: oil immersed current transformer, failure cause , batch defects, disintegration analysis

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